Mofi, thanks for the excellent and valuable empirical information.
Lew, thanks for your inputs as well. I think that you are correct that in MOST cases changing the 47K resistor to 100K would not have any adverse effects on phono stage performance, especially if the input stage is tube or FET-based. But it goes against my technical instincts to incorporate a design modification, albeit a seemingly minor one, without having a full understanding of what the existing design is.
And in particular, I was envisioning the possibility that the active stage at the input may utilize bipolar transistors, and therefore most likely have a much lower input impedance than a tube or FET-based circuit. Conceivably, also, some of the passive components associated with RIAA equalization could be located at that point. I seem to recall having seen some Bryston schematics, for example, to which both of those points would apply.
Finally, given that the cartridge is a MM I would assume that its inductance is somewhere in the vicinity of 100 to 500 mH. That means its impedance at ultrasonic frequencies at which it may output significant energy may be upwards of several 10's of Kohms, perhaps even approaching 100K. That would clearly be significant in relation to the phono stage input impedances we are talking about, implying the possibility (if the input impedance of the active stage is not high enough to be insignificant) that the resistor change could result in adverse effects on noise levels, frequency response, intermodulation distortion, etc.
It all adds up to caution being called for, as I see it. Especially since, given Mofi's experiences and my theoretical speculation (in the other thread), 47K stands a good chance of working just as well or perhaps even better than 100K.
Best regards,
-- Al